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XL472 Left GAM at 1830 today for its new home.
We have two houchin 25’s and another similar power unit, can’t remember the type at Gatwick Aviation Museum. I know for certain one of the 25’s ran mechanically but can’t remember about the other two. We also have houchin 25 manuals which can be copied if required. They are currently blocked in during the reorganisation but I can do my best to get pics and details at the weekend if required.
Dave
Further restoration work has been carried out on XN923, following the engine change much cosmetic and mechanical work is planned.
Last week 923 had cleaning comence of her bomb bay prior to the fitting of a full set of stbd 950 and 1000 lb bomb carriers. This was not made easy with everything having to be passed through the bay access panel due to the bomb bay hydraulics being non fuctioning at the moment as it is stuck in emergency mode, a problem being chased at the moment but with the carriers in its now looking good.




In between carrying out work to finish off the engine change on our S1 Buccaneer yesterday, we found time to carry on with the reheat end of 579. This saw replacement of previously removed rivets and screws at frame 62, some of which had split others we drilled out to removed and rectify corrosion of the magnesium alloy packing pieces fitted between the titanium frame and the aluminium skin.
With the corrosion problem sorted and no damage found to the frame or skin, replacement Monel rivets as per original spec were installed.
Work has also carried on with the re build of the No1 Reheat pipe, with the air motor now unsiezed and operating as per spec.
In between carrying out work to finish off the engine change on our S1 Buccaneer yesterday, we found time to carry on with the reheat end of 579. This saw replacement of previously removed rivets and screws at frame 62, some of which had split others we drilled out to removed and rectify corrosion of the magnesium alloy packing pieces fitted between the titanium frame and the aluminium skin.
With the corrosion problem sorted and no damage found to the frame or skin, replacement Monel rivets as per original spec were installed.
Work has also carried on with the re build of the No1 Reheat pipe, with the air motor now unsiezed and operating as per spec.
Work has carried on with the rebuild of the No 2 Reheat pipe. This has involved setting up the final rigging for the nozzle positions and functioning the Air Motor before connecting it back up to the nozzle position actuating ring and functioning the pipe with a workshop compressed air supply through the closed, cruise, max and min reheat positions. A new nozzle position desynn transmitter has been fitted to the number 2 pipe and function tested. On the aircraft the plug for the transmitter has also been rebuilt and refurbished to match. The No 2 Reheat pipe has now been offered up in preparation for the joining of it to its interpipe, which is required for the ease of installation the whole assembly will then be installed as one.
Various hot air valve wiring plugs in No 1 eng bay have had new pins fitted to the plugs where broken wires had been identified during the rewiring and testing phase. These have now been tested and the cables re-loomed.
Yesterday saw us carrying on with the final split pinning of the fin attachment bolts, re-splicing of the cut fin cables and loose article checks which will continue over the next few weeks before the installation of the No 2 Inter and Reheat pipes.
As we are now approaching the engine installation stage we are actively seeking any Lightning specific ground equipment. If anyone has any such items for sale or that they would wish to donate please contact us.
A lot of work has been on going on 579 the past few months. To start with investigation has been on going into an intermittent problem with the Battery Master Switch, this has on several occasions failed to supply battery power to the aircraft and after checking out and replacing an intermittent battery master contactor and a loose crimp on the master switch the problem has been pin pointed to a slightly dislodged pin in a multipole connector on the aircraft side which will require the ejector seat to be removed and will be tackled in the next month once the weather has settled, a couple more pre existing problems identified and fixed.
The L/H brake pack has been replaced after a leak, attributed to a damaged helicoil insert on the pressure line fitting to the pack. A new pack has now been built up, refitted, bled and function tested satis. The removed brake pack will go back into store and a new helicoil will be fitted in time giving us a serviceable spare.
The Bi-furb or spray mat heater has been refurbished after delamination of the paint due to corrosion. This has now been removed and treated, luckily the heater elements were found not to be damaged and once a checked out and a new coat of paint applied it has now been refitted.
The team took a week off work in Feb to tackle many of the remaining on and off aircraft tasks identified from the Form 700s as outstanding and it was just our luck that that particular week just happened to be the time the snow and a week of bitter winds and sub zero temperatures arrived.
Not to be put off the first job was to sweep the aircraft and surrounding ground clear of snow. Work then began rebuilding a replacement Air Turbine Gearbox (ATGB) assembly, having removed a previously refurbished item as we were unhappy with the level of vibration, the cause of which has been identified and this will again be stored as a spare. With the impellor heated and pressed onto the matched shaft, the rest of the nozzle vane assemble was put back together and the link arm from the governor adjusted and set to rig. It was then time to lug the ATGB through the airframe, fit it and mount the generator and alternator followed by plumbing in all the supply and cooling air piping.
Hot air from our air start was applied to function test the ATGB and get the oil levels correct. The No 1 and 2 engine bleed air connections along with the Reheat Air Motor Control Unit pipes were blanked off and hot air applied to the aircraft. The previously mentioned ATGB nozzle vane governor link was left disconnected and manually actuated to slowly spin up the gearbox to prevent it being shocked into full on load condition straight away. The ATGB was gradually opened up to full on speed level and no vibrations or leaks were found, gearbox install signed off satis.
With the ATGB installation complete this allowed for the reinstallation of the No 1 Interpipe, with a few more bodies available to man handle the pipe in, it was slid into position on its rollers another big piece of the puzzle refitted.
Lightning XM135, inadvertant flight by W/Cdr Holden
Hi Mondariz
Check out thread
http://forum.keypublishing.co.uk/showthread.php?t=20807&highlight=lightning+flight
Dont forget its this Sunday. Work has progressed well since the last night run starting to cure all the little snags shes throw at us over the years of operating her.
WR982 has not been run on a public day for a few years dont miss this one. 🙂
Pembroke Interior
Hi there
Had a quick look at my past Pics could only find this one at the moment will try and dig out some more
😀 Saw her spreed her wings on sky What an achievement! Cant wait to see her on the airshow circuit in the future:)
Hi Paul
It was a few years ago since the Trident and Comet airframes were scraped they were stored for some time on Hangar 7s apron which is now used by Virgin Atlantic. Last I understood was that the Herald was still on charge with some department at BAA and was going to be used as a ground trainer in what role I am unsure, word was also that it could be used by the fire service however they have a purpose built fire trainer now. It was also linked with a move across the perimeter fence to Gatwick Aviation Museum but it seems to have fallen short by less than 20 meters.
Check out previous post on this forum
Shame it seems preserving any aircraft is getting harder work, what with the price of fuel and the dreaded insurance.
Any way wishing you guys and everyone else in the same boat alot of luck and keep up the good work.
Does anyone remember the MK 3 in the US i think painted up in the Coke Cola livery, and was it on the roof of a building??
Hi Peter
With regards to your fuel situation I have heard off Groups using heating fuel as an alternative for Jet A1, for ground runners, is this of any use to you and is it actually a viable alternative for both running and reducing costs??